Part Number:TPS65311-Q1
Tool/software:TINA-TI or Spice Models
please send me the spice model for TPS65311QRVJRQ1
Part Number:TPS65311-Q1
Tool/software:TINA-TI or Spice Models
please send me the spice model for TPS65311QRVJRQ1
Tool/software: WEBENCH® Design Tools
This is my second design LM5141,40V-5.2V DC-DC
I design the EVM refer to the WENBENCH tool schematic
When input is 40V,output is 5.V 3A,IC and MOS are very hot,about 100℃,
Here are there picture about the high and low MOS driver waves,in different output current。
Blue diagram is high MOS driver
Yellow diagram iS low MOS driver
output is1A
output is 2A
output is3A
See the above there picture,when operate the different output current ,the high MOSFET driver open time almost keep unchanged
Let us see the low MOS diver wave changes in different output current
1A
2A
3A
I am in interrogative ,as usual,when the loading is added,the high driver should gain the duty cycle in the buck circuit,Otherwise this state is not my hope, and why only the low driver duty cycle was added when the output current was added 1A to 3A?
I have test the high MOS Vgs,the wave was very strange
It was seen like not as full work,I gusset if it is the reason why MOSFET was very hot,even the output is only 1A
So my main question is something case the IC and MOSFET hot,I hope someone can help me to solve this problem?
I am sure that IC GND is enough,because the IC is not pover device
I found main reason was that high MOS driver is very weak when the input over 20V
like this pictures:
input is 12V,higt MOS Vgs is normal ,IC and MOS can't be hot
input is 30V,higt MOS Vgs wave is Disorderly,IC and MOS are hot
input is 40V,higt MOS Vgs wave is more in trouble
the driver is very weak,so that the MOS be hot when load 。this state I have been understand
But the IC be hot when input is higt voltage,and the driver wave can't serve MOS switch fully,
So what case the IC can't work in high input voltage?
This is my second design LM5141,40V-5.2V DC-DC
I design the EVM refer to the WENBENCH tool schematic
When input is 40V,output is 5.V 3A,IC and MOS are very hot,about 100℃,
Here are there picture about the high and low MOS driver waves,in different output current。
Blue diagram is high MOS driver
Yellow diagram iS low MOS driver
output is1A
output is 2A
output is3A
See the above there picture,when operate the different output current ,the high MOSFET driver open time almost keep unchanged
Let us see the low MOS diver wave changes in different output current
1A
2A
3A
I am in interrogative ,as usual,when the loading is added,the high driver should gain the duty cycle in the buck circuit,Otherwise this state is not my hope, and why only the low driver duty cycle was added when the output current was added 1A to 3A?
I have test the high MOS Vgs,the wave was very strange
It was seen like not as full work,I gusset if it is the reason why MOSFET was very hot,even the output is only 1A
So my main question is something case the IC and MOSFET hot,I hope someone can help me to solve this problem?
I am sure that IC GND is enough,because the IC is not pover device
I found main reason was that high MOS driver is very weak when the input over 20V
like this pictures:
input is 12V,higt MOS Vgs is normal ,IC and MOS can't be hot
input is 30V,higt MOS Vgs wave is Disorderly,IC and MOS are hot
input is 40V,higt MOS Vgs wave is more in trouble
the driver is very weak,so that the MOS be hot when load 。this state I have been understand
But the IC be hot when input is higt voltage,and the driver wave can't serve MOS switch fully,
So what case the IC can't work in high input voltage?
Part Number:UCC28C43
Tool/software:TINA-TI or Spice Models
A buck chopper is modelled in TINA software with UCC28C43. Power rating is 2.5kW. It has to operate from 65% duty to 96% duty @ 80 Hz. Model is successfully built to the requirements. Slope compensation parameters are calculated based on datasheet.
However, while testing the proto, results are not replicated to the simulation. We got sub-harmonic instability in the PWM output. We tried tuning every value of slope compensation parameters, didn't work. Current sensing is placed in switch path in beginning, now it changed to inductor path. Still, same result.
Output voltage voltage is regulated to the set value, throught the duty range, and response is smooth. No overshoots, no Undershoots.
I hope some of you can propose some clues/solution.
Thanks
Ravi
Part Number:TPS7A1601EVM-046
Tool/software:TINA-TI or Spice Models
Need SPICE model for simulation in PADs AMS
Part Number:TPS55340-Q1
Tool/software: WEBENCH® Design Tools
Hi
This is my first time working with Webench.
I created a design with the TPS55340-Q1 and would like to make a PC board but there are a few conflicts.
Looking at the WebTherm Simulations, D1 is incorrectly oriented on the board. Also the Board Layout from the cad file export
area is also incorrectly oriented and missing solder pads even if it would be rotated. In Cadsoft Eagle software the top placement layer
as well as the bottom placement layer have been removed so I am unable to alter the board myself.
I have not been successful in being able to talk directly to a TI support person. Does anyone know
of the path I should take to get this resolve so I can proceed with my project.
Thank you
Ralph
Part Number:LM5022
Tool/software: WEBENCH® Design Tools
Hi, can anyone help me out in a design of boost converter. the input voltage is 12-13.5 volts as output is 180 volts maximum output current is 150mA here i have achieved those but the problem is mosfet. The mosfet i am using SIHB11N80E which is greater specs. the design recommends Vds 250 volts and current 3 Amps but it is having 850 and 8 amps respectively. The mosfet is getting too hot when boost converter is on load either load is low or high. Help me please thanks is advance.(Please visit the site to view this file)
Part Number:PMP9484
Hi, I can see that the NMOS CSD18501 (Q1) used to drive the stepup is used with negative bias. Is that
correct? The back diode will thwn transfer the durrent i the second phase of the stepup.
Part Number:DS99R104
Tool/software: WEBENCH®设计工具
Hi All,
17pin LOCK does not receive Sony's optical drive chip (CXA3856), what will affect,By the way, is the schematic correct?
Part Number:PMP11208
Tool/software: WEBENCH® Design Tools
Need design information to do power supply in region 220-250A at 0.9V.
Part Number:TCI6638K2K
Tool/software:TINA-TI or Spice Models
As per TCI6638K2K IBIS model, We have 9 driver strength like below, But SW team able to see only 34 & 40 ohms and not able to find the 50 ohms driver in SW.
Please let me know how to finding the 50ohms driver. As per our board topologies, 50 ohms driver strength only passing the results.
Regards
Karthik
Part Number:TPS54350
Tool/software: WEBENCH® Design Tools
can you send me the schematic for the voltage regulator for input 9V-20V for the output of 5V and 2A using the tps54350 ic. There is no web bench schematic for the regulation using this ic. please if you can, send me the schematic for the above-mentioned voltage and current values.
hi..
How to apply for the in person training on Smart glasses application design in India?
Tool/software: WEBENCH® Design Tools
Hi,
Do you know any meter to read 400v DC.
And 30 AMp current?
Thanks
Part Number:TIDA-01022
do you have users guide for TIDA-01022 to explain the function of connectors on the board?
Part Number:TPS56428
Tool/software: WEBENCH® Design Tools
Hi ,
We have used the part TPS56428 in our design to generate 4.2V output from 5 V input and its working fine.
But if I check the same in the Webench tool, the following error pops. Kindly help me with this.
Error:
We're sorry, we could not find a solution to match these requirements for the following reason(s):
Calculated duty cycle exceeds limit
Regards,
Abhilash G
Tool/software: WEBENCH® Design Tools
I seem unable to identify and leverage the tool to identify and generate a reference design for a DC-to-DC converter with the following requirements...
Vin = Min. 10V DC; Max. 36V DC
Vout = +/-15V DC Max. 3A
Can TI provide assistance and/or guidance?
Thanks,
Part Number:TIDA-01022
The U24A at page 13 has 2 sets of input for the CLKIN1P/N. First one is from CLK-IN* over the T3. The second one is from CLK-IN* over the U74 (NB7V33MMNTXG) at page 14. they both are available.
Part Number:TIDA-01606
Could you please give me the code composer codes related with this design